We are in preparations to be at the 2017 LA Roadster show in Pomona, CA at the Fairplex on June 17-18th (Fathers Day weekend) in two locations this year. We will have our indoor booth again this year, but will also have a spot out in the swap area.
So far we plan on bringing out three ’32 frames with our full X members with show pricing. One will be pinched for 28/29 Model A use. We will also have our accessory K-member legs, stock style brake pedal sets and other bolt on chassis parts.
If you want to pre-order any of the product and have us deliver at the show, give us a call @ 866-553-8996
As promised earlier, we have the 57-60 F100 and 55-59 GM truck Dakota IFS kits available in the store. These are for the stock arm Dakota suspension systems. If you want air bag systems, any of the kits that would fit any of the Dakota two wheel drive systems should work in our kit. However, we are getting hit pretty hard to do a dedicated IFS kit with tubular control arms and air bags. So we are going to do our best to get them drawn up and in production before Christmas!
Also in the works are engine mounts for the Dakota IFS kits. I think we have the Chevy engine mount systems ready to go and will be in the store in a few weeks. The Ford Windsor style mounts are still in need of some work to make them what we want. And if we can, the LIMA series (429-460) engine mounts also. These of course are going to require a rear sump oil pan to clear the rack and pinion like any other IFS kit on the market.
Keep an eye peeled for our new line of rear suspension kits too! There will be three kits ranging from near stock to work with your nearly stock Dakota IFS and a lowered kit as well as a hammered kit with a 5 plus inch C-notch built into the boxing system. These kits will be an un-parallel and unequal length four bar with a panhard rod. A moderately low roll center that works with pickups and all come with 100% anti-squat at ride height and minimal changes in pinion angle to curb any driveline vibration. Heavy duty construction with greasable polyurethane bushings and RideTECH shocks.
We are also working on the ’32 Ford chassis components, The front and rear bolt in crossmembers should be in production by mid-January. We are also considering a full bolt in X-member similar to our ’32 system for the 33-34 Ford frames. Let us know in the comment section what you think and what you would like to see in that kit.
What a show. The heat had to be a factor in the low turn out. That and the guys that go in first roped off over 90% of the spaces, leaving many swappers to turn around and go home. I spoke to two guys that demanded their $70.00 back because there were no available spaces. Even on Saturday a large percentage of the “saved” spaces were still empty with yellow tape and cones and maybe a lawn chair and a small pile of scrap metal to guard the space. I cannot see this happening for much longer before they the LA Roadster guys start having to do assigned spaces or at least check that the guys that paid for one spot only have one spot and so forth.
We set up with Hotrod Ron and had a good selection of stuff. The reception to our new fully bolt together ’32 frame was encouraging. The SBC engine saddle was the hit of the show! Now I’m going to have to put them into the store. Look for those items in the near future, but if you’re impatient you can always give me a call.
We talked with several satisfied customers and even saw Tim Thompson and his wonderful ’32 3W with the first mail ordered Full-X member installed. Of course Dr Marvelus and I had to take the opportunity for a shot of us all together.
It’s summer time and we are still at it. More new products are on the way.
Latest out of the shop is Ray Castor’s 1957 Oldsmobile. Ray brought us this car last year just before we got really deep into the 51 Chevy PU For Metro AA. It initially came in for some front suspension work. As we are to understand this car was purchased from Desert Valley Auto, same guys with the TV Show. It had already been sand blasted, painted and subframed with an early 80’s GM full-size clip. Most likely an Oldsmobile because ray told us it had an Olds 455 in it. He found a 1958 Olds 371 J2 engine and trans, had it rebuilt and installed by yet another shop. The problem came when he went to put his tires on it, they didn’t fit under the fenderwell very well at all. The tires actually stuck outside the fenders by a half inch or so and the front crossmember was less than 2″ off the ground.
So the first thing to determine was what condition the car was in and what we could do to fix the botched front clip installation. On tear down things became very evident that the persons installing the clip made more than a few mistakes besides choosing the wrong clip for the car.
The entire clip besides being mounted very low on the chassis, was off center a bit and the right side spindle was a full inch behind where it should be as well as being a few degrees off, lower on the Left side. You can see just how high the engine was placed in the chassis. So high in fact that the installer trimmed the upper webbing out of the center X member for transmission clearance. The wobbly engine mounts were pretty comical too. It was about at this point we realized just how hard of a hit this car had taken at some point. There was evidence of a fairly severe diagonal in the whole car.
Next move was to get it on the chassis table and square it up, then start the decision making on what to repair this car with. Of all the choices available, one stood out as something new for me to try. The late 70’s to mid 80’s Jaguar XJ sedan. My friend Scott Zekanis did a similar installation on his 1957 Buick sedan a few years back and has had good success with it. I did my research and found that the Oldsmobile is less than 100 pounds heavier than the Jaguar and had very similar weight distribution. Plus the track width was in the range we were looking for. The stock Olds front had to be close to 59″ wide. The rear axle was right on the money at 59″ so it stands to reason at this point in automotive history that the track widths matched, that and a bit of careful tape measuring and internet sleuthing.
A few phone calls and internet searches, I had myself a line on a 1985 Jaguar XJ6 Vanden Plas. Nice enough car and the price was more than good. Time to strip both cars down, Ray made the decision to use both the front and rear suspensions from the Jaguar (good choice!) as the rear axle in this car was also an unknown. It was stock but if the car was wrecked pretty bad, there might be issues with bent axles or what not. Besides, it just made perfect sense to do a fully independent suspension. Brian and Dr Marvelus AirArced the front clip off after locking the car to the table and Brian and I also disassembled the front and rear subframes from the Jag.
Pressure washed clean and time to start figuring out how to make this all work. This was more work that any of us figured. Still not sure if dropping the engine out the bottom was a good choice or not. Regardless, it came apart and the suspension was pretty decent.
Old clip off, Jaguar front mocked into place, I made my measurements and drew up new frame rails in my 3D software. Made the decision to use as much of the stock Jaguar suspension components as possible. This meant also rubber mounting the front and rear suspensions to give the old Olds the best ride quality possible.
One of the things that was going to make this a difficult build was the owners insisting on keeping the Factory AC and heaters in place. If you will notice the large black box where we would normally hang a power booster from, that is the AC Evaporator case. This didn’t cause us problems for the frame and engine placement.
Front end finished to a stopping point, we turned our attention to the rear suspension. It really surprised us how well the whole Jaguar IRS fit while still in it’s cage. I determined that to rubber mount the stock Jaguar rear cage, a section of frame rail would need to be replaced and a bit of the trunk floor coped in for the new bit of frame rail.
The stock Jaguar trailing arms are critical if you intend on rubber mounting the cage like we did here. If you leave them out you will get some serious tire shake or worse. We also installed this rear axle with 3º of pinion up which goes against all the internet experts out there. I am not willing to just follow trends, so actual investigation went into doing this. The three degrees up not only allowed for a better driveline angle for our universal joints, it also gave us a tiny bit of anti-squat! Yeah, traction is cool!
The wrap up was fairly boring stuff, rush to finish meant the camera phone was in my office out of harms way for the most part. We had a custom made radiator done, rebuilt the core support, ran brake lines, installed a hydroboost system with the stock Jaguar master cylinder under the floor, built an exhaust system that snaked it’s way through everything and made engine brackets to hold the air compressor and alternator properly. Didn’t get any final pictures before it left, but if you attend the Goodguys shows, you are likely to run into this car.
The little bit I got to drive the car was pretty darned cool. Very smooth, very controlled. I think once Ray gets the engine and transmission sorted out, he is going to have one hell of a daily driver on his hands. You can say I am a believer in the Jag conversions. Not an easy job compared to other popular choices out there, but for an ambitious home installer or a customer that wants pretty much the best of comfort and good handling this is a solid choice.
As started by yet another shop in town and resultant failure to build a sound foundation, this 1951 Chevrolet 1ton was altered, shortened and modified into a mess of a chassis. Way past budget and nearly two years after it was commissioned the truck ended up on my doorstep. What showed up was powdercoated in a grey and black hammered finish. The weld porosity was clearly visible through the coating, the rails were not straight and every hole to attach the body, bed and running boards was welded up and boxed to prohibit future attachment.
Not only was the frame not square or true, the front end was un-alignable, no mounts for the coil overs on the lower control arms, the rack was offset to the passenger side over an inch. It took 5/8″ shim to get the left side to align and no shims in the right I still got over 1/2º positive Camber and only 1º positive Caster. Because of the offset of the rack and it’s misplacement, the front end had a pretty severe bumpsteer on the left side and a proper connection between the rack and the spindle on the right was not possible without inches of toe out.
The rear suspension was so poorly installed that the bars could not be installed without forcing things into place and the coil overs were in a serious bind if the rear was adjusted for proper pinion angle. The panhard rod was also too long and so far out of alignment that it couldn’t even be forced into place. Even the rear axle housing was warped so bad that the axles didn’t fit properly and would have caused some premature wear issues.
The center tubular crossmember was insufficiently installed and triangulated. It provided no resistance for vertical support of itself nor for twist or beam resistance. Not even the forethought to support the transmission, it just took up space and added weight.
The decision was made to pretty much scrap the whole frame. We sent the frame over to our powdercoater to have them bake the coating off and sand blast back down to good metal. I don’t know if anyone has ever done it, but welding on anything with powdercoating is nasty stuff. What we got back shocked us even more, there were sections of boxing plate and front suspension crossmember that were not welded at all, others so poorly welded they were doomed to fail. No choice but to cut it apart.
Once down to bare rails Dr Marvelus and I commenced building some fixturing to hold the rails in place. This is where we spent far too much time on this build but we have some solid frame building gear to build the next one of these frames that come through the door. This also helped us get the frame rails straight and true, I believe the Dr spend nearly a week stripping and straightening to get to this point.
This was a 1Ton frame, so the shape is slightly different and the arch over the rear axle was much lower and didn’t allow for sufficient axle travel at the ride height we wanted. After a mockup of the body, bed, fenders and running boards we determined how much more arch over the axle we could use. We documented the important stuff and I drew up some new frame parts, cut and the good Dr MIG stitched them together and finished them to a stamped clean finish before grafting the new arches into the frame. Meanwhile I went about the front end, the stock front horns of the frame rails were absolute trash. Bent, welded and twisted out of working condition I decided to build new rails, but make them parallel from the firewall forward. I did similar on other trucks like the one we did for the Dynacorn Corporation, it gives you quite a bit more room for engine mounts and accessories as well as steering and so on.
I’m trying something a bit different with my boxing plates these days. Instead of the traditional plate or stepped-in boxing plates, these are C-shaped and thicken the frame rails to 3″ wide. The thicker frame rail will be much stronger and because of the lap joint, bowing after welding should be kept to a minimum, stronger weld and almost no finish grinding is necessary.
Next up was getting the front suspension in place and the center tubular crossmember. The front end is late C4 Corvette, fully polished and has Global West Del-A-lum bushings installed otherwise stock. The rack is FOX platform stuff and I had to render everything in my software to determine the geometry. The goal wasn’t ultimate handling but a good compromise between good handling and ride comfort. I think I found a good mix that keeps the roll center near ground level, has reasonable camber change and of course near zero bumpsteer. I could not dial it all out because of the FOX tie rod ends. Then I could go about designing the crossmember to hold it all in place.
The tube center X-member and integrated transmission mount got bent up, coped and TIG welded together. Note the lower two tubes of the X-member are parallel. This makes transmission swaps possible without having to fabricate new mounts. The trans mount itself has an offset to it so that a slight tap and twist counter clockwise lets it drop right out of the structure. If it didn’t, it would be very difficult to remove it.
The rear is a triangulated four link, designed to be close to the 100% anti squat and adjustable somewhat for pinion angle and centering. Nothing too special, just repurposed TCI parallel four links in stainless. We used the lower bars as is but shortened the upper bars to 17″. I fabricated a new crossmember to transition the frame rails at the front attachment point of the four bars. additional crossmembering for the four link to attach and to stiffen the frame rails.
The old narrowed housing was out of alignment and was in sad condition that we were asked to retube it. The rear axle housing was completely TIG welded and I made custom brackets to hold the lower bars and coil overs. Dr Marvelus made the upper bar tabs. The last bits were fabricating motor mounts, upper control arm mounts and coil over mounts then we went in in a flurry of activity. Then two intense days of TIG welding to finalize everything as it came out of the frame fixutring and became a roller.
If you would like to see all the details I took photos of, click here
The rolling chassis complete, we are moving forward with the build. Right now we are adding exhaust, fuel tank and fitting the cab to the frame. Stay tuned for more updates!
The story goes like this, Mr Funk called my sidekick Dr Marvelus on a late Friday night just after picking his “Rat Rod Hudson” from another shop here in town. Mr Funk was pleased as punch to get it on the road after his two year build process and many foldable greenbacks, but was absolutely terrified by what he now owned. The good Dr told him to bring it in Saturday morning.
What showed up on my doorstep may just be……. I digress. On with the story.
Lets back up a few hours, yes hours.
Upon picking up his car, the owner at Puerile Customs told Mr Funk to take it easy, don’t go out on the highway and learn the car because its a bit of a handful. Mr Puerile assured Mr Funk that the car was sound and he “stood by” his work. By Mr Funk’s account this car needed your undivided attention 100%, no taking your eyes off the road even for a second to look at the oil pressure or temp gauges. He was uneasy but had no major complaints as he drove his car home. Enjoying his conveyance it was time to hit the local, ahem, pub. Mr Funk recounted a tale of showing off his new joy to some colleagues and after some good natured ribbing and displays of encouragement, Mr Funk stepped on the gas and the trouble began.
The car careened in an uncontrollable manner and started the dreaded “death wobble” with the brakes applied at maximum sphincter gripping pressures, nothing happened. No control, four lanes of traffic were crossed before the car came to rest. Now terrified, Mr Funk made the call to Dr Marvelus.
And so, this is what landed at my doorstep.
Initial inspection, the drastic negative Ackerman, Model A wheels and steering location warranted a closer inspection. There was quite a lot to take in. Someone had obviously spent some time trying to produce something that would stagger its onlookers.
This car is definitely not HAMB material. Certainly not worthy of our notice. A breed that deserves our disdain and upturned noses. However there is a lesson to be learned here, an example needs to be made of those who have wronged Mr Funk and an opportunity for myself and Dr Marvelus to showcase our finely tuned skills and abilities.
Let me bore you with the intricate details of this so called “rat rod” shall we?
This first set of pictures is from my initial inspection, all I was truly concerned with was the condition of the front suspension and why it had the guidance system similar to that of a Scud Missile.
The first thing to draw my eye was the steering linkage, made up from pipe wrenches and connecting rods with a few machined bits thrown in for good measure. The steering box is a Saginaw 525 possibly from a Jeep because it takes 6.5 turns from lock to lock. The box mounted on studs just aft of the radiator were not sleeved. The holes were near edges and the plates were not fully welded. The steering shaft back to the steering wheel consisted of welded couplers, universal joints and a stub shaft from a VW bug mounted in a single bushing hanging from the dash. No substantial support left the steering wheel a bit flaccid. I apologize for letting that tidbit escape my camera’s eye.
If you would take notice, the welds holding the pipe wrench to the steering system in the above pictures. Notice how over temp and undercut the welds are.
I broke that bit off with a two foot prybar and about 30 pounds of force.
The next bit of bother was the tie rod. Most of you fine chaps know that mounting the tie rod out ahead of the axle is not always the best solution to your problems. However when building a “rat rod” getting the car as low as possible is your only concern. This means placing the front beam axle ahead of the radiator. This not only allows the lower tank of the radiator to be as low as possible, but also nudges the front axle out for at least another foot of wheelbase. This leaves the problem of what to do with the tie rod. Behind the axle is an issue as it interferes with the radiator and it’s rakish angle so your best bet is to flip the steering arms around front. If Mr Puerile had known about the work done by Mr Rudolph Akerman he could have avoided this folly into a steering system that caused the vehicle to push so severely that turning the wheel to full lock had a turning radius somewhat inside that of the Queen Mary.
The steering arms you see are most likely from a 1953-1956 Ford F100. Wait for the more creative uses of more of this donor vehicle.
Not truly concerned with the air spring mountings or any of the other gear, Mr Funk and I agreed to a figure and the vehicle was left to me. I pulled the vehicle inside my shop. It took me 20 minutes to achieve this due to the small 8′ door and 90º turn to enter the shop.
I shut the doors late Saturday night and left the little Hudson to think about where it had been. On the following Monday when I opened the doors and flicked on the lights the little Hudson greeted me by pops and creaks. It was resting firmly on the ground and the air pressure in its scuba tanks was at naught, but still, the suspension was so bound up that it continued to settle over 24 hours later.
The entire air system would not hold pressure for more than 20 minutes. In fact, it leaked so badly that it needed adjustment every 5 minutes or so just to maintain altitude.
And on to that. In adjusting the suspension from drivable to flat on the floor was not even remotely smooth. It did take a considerable amount of time to build up enough pressure to overcome the sticktion of the suspension mountings. And it was not easy to replicate the driving position. Dr Marvelus and I donned our handschuhes and went to work.
We found many things awry, the connecting rod bell crank system was merely hand tight, without any manner to keep the Grade 5 bolt in place that acted as the pivot. No inner sleeves, no bearings or bushes. We now know just some of what caused all the creaks and moans.
During dissasembly we notices several of the “welds” were poorly executed and were already showing cracks. The problems were mounting up and the agreement I made with Mr Funk were starting to fall out of favor with me. But a deal was struck and I needed to stick to it.
As the dismemberment went on and I was cooking up a plan on how to save this car for Mr Funk more exciting fabrication work was found. The good Dr and I assume that this car was concepted and built by stacking items against each, on the floor, other until pleasing to the eye then scraps of metal and what ever was lying about were used to make connections between the aforementioned items.
I reviewed what lay before me with the intent on just trying to fix what was here to make the Scud-Hud safe and reliable but was stymied at every turn. I could not find a frame or fitment satisfactory. My options were dwindling and knew I was just wasting time and energy. I decided that everything forward of the cowl was a lost cause. Nothing save for the brakes, spindles, HEIM joints and air springs themselves were about the only items worth salvation.
I went through quite a process to create a whole new front section of frame. I was unsastisfied with the look and condition of the 1941 Ford front I-beam axle and decided to trade Mr Funk one of my standard Model A axles. I also wanted to improve the pedigree of the old rat to a more upright citizen of the motoring kind. This meant standing the radiator and shell proper upright and rearranging a few items bringing the car into fine shape rather than the slough it was mimicking.
Firing up my digital computing machine and manipulating my figments the new front end started to grow on my screen. New formed frame rails with giant speed holes to help shrink the overall visual size of this car, it is rather large. I also placed a facsimile of the Model A axle and placed new connecting links and “batwings” to hold all the various bits in place as “traditionally” as possible given the circumstances.
Rumaging through my pile of cast offs I found a set of Delco Lovejoy shocks from the rear of a 1938 Cadillac that were in fine sporting condition and though they would be a very nice addition to the front of the Scud-Hud. As the car had no shocks front or back and the nature of the “suicide” mounted front mounted axle tends to not be friendly to airplane shocks. The long lever shocks could be mounted on the flanks of the frame rails with their spindly arms reaching forward to the axle.
My intent was to clean the lines of the new front frame section and draw your eyes away from the tidbits that were visually unappealing. The placement of the Cadillac engine afforded me just a bit of space behind the engine mounts to create a location for mounting the somewhat repulsive air springs. To connect the axle to the air springs I created a shaft and lever system mounted on bearings. This gave the appearance of torsion bars, a much more accepted look to the discerning Trad-Rodder.
Just installing simple levers did not satisfy my visual intent and did not articulate the air spring properly. I tipped the air springs outboard by 30º and created an unequal length and nonparallel linkage system that pushes the top of the air spring reasonably close to the the 30º line the air springs are mounted on and this also gave me the opportunity to use longer bellcranks for the leverage ratio I wanted. As an added bonus, I could install a polyurethane bumpstop under the upper control link and make it adjustable if needed to prevent the newly built vehicle from actually touching the pavement.
The clevises used in the four link bars are common rod ends available from my favorite hardware dispensary, McMaster-Carr. The ends are attached to the fabricated “batwings” using large shoulder bolts and PEEK plastic bushings That allow rotation in one plane. Using a HEIM on this end would not work properly as the weight of the car is going to be hanging from the batwing and a few inches aft of the axle. There will be forces to pull the batwings inboard, this arrangement of connection will hamper this action.
While I was designing the save for the front half of Mr Funk’s Scud-Hud, he had a conversation with Dr Marvelus about repairing the less than satisfactory body panels and possibly taking care of a few more items on the car. I was waiting for materials and supplies to show up so in order to keep things moving along, the good Dr Marvelus sheared up some sheet steel and went banging away.
As the materials showed up, I processed the solid model drawings I had made into a language understood by my plasma machine. Cut the parts and started to assemble the individual components to make up the front clip.
I spend some time machining tubes to accept the bearings of the lift shafts and securely welding them into my motor mount/air spring structure and radiator core support.
And Dr Marvelus attacked the rear with a new apron to cover the Scud-Hud’s neither regions.
More parts added into the mix and the front half of the frame is taking shape. The four bars are fabricated using 1.25″ X .125 DOM steel tube for the uppers. The 1″ clevis at the front and the salvaged 3/4″ HEIM at the rear. The lowers are 1″ X .125 DOM steel tube with a 3/4″ clevis at the front and a 5/8″ HEIM at the rear. The linkages connecting links from the shaft bellcrank and guide link have bronze bushings and sleeves to allow free but controlled movement. The front of the lift shafts are connected to the batwings using standard 1.75″ spring shackles.
The day came and the Scud-Hud was to become a bit more Sir and a bit less Rat. Dr Marvelus and I scuttled the Hud from the two post lift to the fabrication table and continued to centerline and level the Hud out. Clamping it to the table we realized how out of square the frame was, twisted and deformed. The engine and trans were pulled from the solid mounts and the cutting began. The weld slime was removed and the remaining frame chunks were trimmed to a reasonable size and condition for me to attach my new front frame section to.
Mr Funk asked me to inspect every element of the car to ascertain the proper function and serviceability. While assembling the front suspension to set up the new steering arms, I needed to remove the brake rotors from the spindles. Upon pulling the dust caps I found blacked grease. I am familiar with the type of grease, it was Lucas Red Tacky and was gritty and burned. Not only that I noticed there was not a tang-washer in sight! This was a disc brake kit ordered directly from Speedway Motors and I would be a bit dismayed that the kit did not come with one. Regardless of whether it was supplied or not, there was a machined and zinc plated spacer between the outer bearing and the spindle nut.
I inspected the bearings, there was a liberal amount of grease applied to the spindle stud but superficial amounts were packed into the big end of the rollers. It also appeared as if the protective coatings the bearings were shipped with was not removed and this contaminated the bearing grease. Moving on from that, I fitted the king pins to the new Model A axle and modified the Speedway caliper brackets to work with the CE bolt on steering arms and cut and threaded a proper tie rod.
It was about this time when I realized what type of vehicle these RadRodsters are trying to emulate, I think they are enamored with the Fuel Coupe but just miss the mark by a bit.
It was about this point where Mr Funk reached his ultimate frustration with the Scud-Hud. He wanted Dr Marvelus and I to remove the silly ammo box wiring control system, seats and expanded metal drive shaft tunnel to get the floor out. At the same time to investigate why the rear axle was offset to right by over an inch.
What we found made us quicken our pace at deconstruction. There was literally everything from a dollars worth of Nickles to exhaust U-bends, Rebar, All Thread and multiple layers of scrap metal that made up the floor. All manner of square tubing and plate was used to weld the rotten body to the frame. Two flex plates copped it for the seat mounts and they were cut in half so haphazardly that who I assume was Mr Puerile that had done this work, filled over a 1/2″ gap with MIG weld to attache the half flex plated to the 16 gauge sheet metal floor.
Now we were getting down to the meat of the matter. Just how so much of this car got off track and why so much was out of square. The frame rails were tapered, narrower at the front than the back under the body. However, the builder squared the crossmember tubes to the right side frame rail making the cross beams not square to the centerline of the car. This mistake was further compounded in the rear kick up that supported the entire triangulated four link system. While the brackets were close to correct on the axle, the frame they were attached to were not.
My judgement was to cut the rear kick up off and the last rear cross beam and try to rebuild the frame from there back. After deconstruction it was clear that there was no saving what was left without many hours of laborious work and for little gain. It all had to go. Out came the Air-Arc to remove my clip from what was left of the sorry frame.
Back to the computer for me. I had to construct a simple and cost effective frame that would actually work well with what I had already created but didn’t rupture Mr Funk’s wallet. I also needed to reuse as much of what already existed and keep it all under the envelope of the body. I regret my decision (you will see later) but the end result works quite well and Dr Marvelus and I can finally cut this project short and get back to repairing.
I chose a triangulated rear four link system with a air spring mount that keeps the end caps of the bellows parallel to each other.
While doing my set up for the upper bars of the four link system I found the last bit of rubbish I had to deal with. While the lower fourbar/coilover brackets were at least centered on the housing, they were not clocked properly. The right side bracket was at least 15º forward of the left side. This pushed the rear axle back over 1/2″ on the right. They had to come off.
The lower bars of the rear four link are a bit complex, but considering what I am going to ask of them they will need to be heavy duty. The sides consist of 10 gauge Cold Rolled steel plate, machined bushings and a length of 1.25″ CR Bar threaded with 3/4″ 16 on the end to accept the Heavy duty HEIM end. Then the rest of the assembly came together rather quickly. Upper bar and bellows mounts, and damper strut mountings.
I reversed a Corvette steering gear I had lying about and attached it to a mount sprouting out the back of the left front frame horn and then fabricated a new steering arm to finish up the front. A set of engine mounts and transmission pad to tie up all the loose ends before disassemblely and final weld out of the frame.
Off the table and onto the floor for another mock up. This time with the new wheels and tires, no adapters and a whole new attitude. These last few shots are without the bumpstops in place, so yes, the frame can touch the ground. With the stops in place it cannot.
There is still quite a bit for us to do yet, but for now it’s off the table and is ready for true progress for a total redemption. While it may not be your style of car, it will be a sound and safe driving car with a flair.
Dr Marvelus and I will be repairing more of the bodywork, installing a true floor that seals out nature. As well as adding a few styling cues that will help prevent the Scud-Hud from being terribly dated and keeping Mr Funk happy for miles to come.
The project took a turn, Mr Funk didn’t want to spend the greenbacks to properly repair the Hudson body. It was discussed that if he could find a better body with a bit more value it would be in his best interest to do so. He found a very rough 1931 Model A coupe body with a horribly botched chop and quarter repair. This is the body that the car left with. I will do updates in a while.
I am just bringing this up because someone brought it up on the HAMB today.
Bruce had bought a kit from Morrison A&M for his truck and had done the majority of the installation himself. He didn’t realize just how much work those universal kits take to install. So he contacted us to check his work and if it was good to TIG weld everything in place. When he dropped it off, we discussed what had been done and what needed to be done. The frame still needed boxing plates for the front and for the rear plates to be final welded. I offered to build a tubular crossmember system just like the ones we built for our frames and Bruce went for it.
Brian and I set off on a metal flinging frenzy of crossmember removal, cutting, grinding and tube bending. A bit more measuring and I placed the engine and trans then fabricated a nifty set of engine mounts that clear the steering rack and pinion. Thirty plus hours later, we had this!
The first Oldsmobile overhead valve engines are definitely one of the coolest, vintage engines you could put in your hot rod. The availability and variety of accessories makes the early Olds a winner in our book but mounting them can rack the brains of the novice installer. The stock tricycle mount works fine if you have a stock trans, however, if you don’t want to run a Hydro your engine mounting scheme hits a brick wall.
Ross Racing Engines has provided some stellar adapters to mount manual and modern GM transmissions to these engine. We use one of their adapters in the current ’31 Sedan build using a Tremec TKO 500. The loss of the stock Hydro means the loss of the rear engine/transmission mounts. It makes sense to use the mounting pad on the Tremec and mount the engine more conventionally. This was the idea behind the vintage Hurst mounts, we went a slightly different route. CNC cut from 1/4″ steel plate, formed and TIG welded, we picked up the stock engine mounting holes in the timing cover. The mounts are made from Energy Suspension universal polyurethane mounts, we machined the aluminum cups to restrain the bushing and add a bit of class. These will get polished and the mount will be chromed.
So if you are interested in something like this for your own project, we made a few extra. They are in the E-store in plain or chrome!